Kyle W. Colley Wrote:
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> I was working on that train. The hat nut on the L1
> drive wheel was missing and the rod was sliding an
> excess of three inches off the wheel. Our options
> were to take off the rod from the 1st and 2nd
> drive wheels on both sides, or to run down with
> diesel. The roundhouse decided that we should not
> run down without side rods, so we switched out for
> a diesel (which was luckily already in Silverton).
Thank-you Kyle for the description of what happen. When I read the newspaper today and they posted the pic with just a brief caption made me curious. No slam at D&S or equipment was intended. Thank-you. Larry